News & Comment

AAIB Report on 2013 Sumburgh Helicopter Accident (CHC Scotia AS332L2 G-WNSB)

Posted by on 1:53 pm in Accidents & Incidents, Crises / Emergency Response / SAR, FDM / Data Recorders, Helicopters, Human Factors / Performance, Offshore, Oil & Gas / IOGP / Energy, Safety Management, Survivability / Ditching

AAIB Report on 2013 Sumburgh Helicopter Accident (CHC Scotia AS332L2 G-WNSB) The UK Air Accidents Investigation Branch (AAIB) has published its report into the 23 August 2013 accident were CHC Scotia Airbus Helicopters AS332L2 Super Puma G-WNSB impacted the sea on approach to Sumburgh Airport in the Shetland Islands.  The AAIB report is 266 pages long.  This article is intended to highlight some of the key aspects of this comprehensive report. The CHC helicopter, chartered by Total, was making a 3 sector flight to Aberdeen from the Alwyn North installation in the East Shetland Basin, via the Borgsten Dolphin drilling rig and Sumburgh (for a refuelling stop, following a relatively late manifest change to add an extra passenger on the return flight). The helicopter capsized and four passengers died, the first fatalities in a survivable water impact of a helicopter on the UK Continental Shelf since the Cormorant Alpha accident in 1992. The Crew The G-WNSB Aircraft Commander was an experienced Super Puma pilot who had approximately 15 years experience on the L1 Super Puma [sic] and 3 years experience (1894 flying hours) on the L2 Super Puma. The Co-Pilot had been a flying instructor on single engine, single pilot aircraft at a different company with approximately 3000 flying hours but was new to Super Puma operations. He had been with the company for only a year, initially training on 225 Super Puma but then retrained onto the L2 Super Puma, qualifying in February 2013. The Co-Pilot had approximately 400 flying hours on the L2 Super Puma. The Accident Flight Meteorological data for Sumburgh at the time indicated broken cloud at 300ft, with 2,800m visibility.  The AAIB say: The commander was the Pilot Flying (PF) on the accident sector. The weather conditions were such that the final approach to Runway 09 at Sumburgh Airport was flown in cloud, requiring the approach to be made by sole reference to the helicopter’s instruments, in accordance with the Standard Operating Procedure (SOP) set out in the operator’s Operating Manual (OM). The approach was flown with the autopilot in 3-axes with Vertical Speed (V/S) mode, which required the commander to operate the collective pitch control manually to control the helicopter’s airspeed. The co-pilot was responsible for monitoring the helicopter’s vertical flightpath against the published approach vertical profile and for seeking the external visual references necessary to continue with the approach and landing. The procedures permitted the helicopter to descend to a height of 300 ft, the Minimum Descent Altitude (MDA) for the approach, at which point a level-off was required if visual references had not yet been acquired. Although the approach vertical profile was maintained initially, insufficient collective pitch control input was applied by the commander to maintain the approach profile and the target approach airspeed of 80 kt. This resulted in insufficient engine power being provided and the helicopter’s airspeed reduced continuously during the final approach. Control of the flightpath was lost and the helicopter continued to descend below the MDA. During the latter stages of the approach the helicopter’s airspeed had decreased below 35 kt and a high rate of descent [up to 1,800 fpm] had developed. The decreasing airspeed went unnoticed by the pilots until a very late stage, when the helicopter was in a critically low energy state. The AAIB characterise this as “consistent with entry into a Vortex Ring State,...

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Germanwings: Psychiatry, Suicide and Safety

Posted by on 8:04 pm in Accidents & Incidents, Fixed Wing, Human Factors / Performance, Regulation, Safety Culture, Safety Management

Germanwings: Psychiatry, Suicide and Safety The French Bureau d’Enquêtes et d’Analyses (BEA) has issued their report into the loss of Germanwings Airbus A320 D-AIPX and 150 lives in the French Alps on 24 March 2015, which was due to the actions of the Co-Pilot.  Below we focus on the highlights from the 110 page report. The Co-Pilot The BEA summarise the career of the 27 year old Co-Pilot Andreas Lubitz as follows: between January and April 2008, he took entry selection courses with Lufthansa Flight Training (LFT); on 1 September 2008, he started his basic training at the Lufthansa Flight Training Pilot School in Bremen (Germany); on 5 November 2008 he suspended his training for medical reasons; on 26 August 2009 he restarted his training; on 13 October 2010, he passed his ATPL written exam; from 8 November 2010 to 2 March 2011, he continued his training at the Airline Training Centre in Phoenix (Arizona, USA);  from 15 June 2011 to 31 December 2013, he was under contract as a flight attendant for Lufthansa while continuing his Air Transport pilot training; from 27 September to 23 December 2013, he took and passed his A320 type rating at Lufthansa in Munich (Germany); on 4 December 2013, he joined Germanwings [a Lufthansa subsidiary]; from 27 January 2014 to 21 June 2014, he undertook his operator’s conversion training including his line flying under supervision at Germanwings; on 26 June 2014, he passed his proficiency check and was appointed as a co-pilot; on 28 October 2014, he passed his operator proficiency check. The BEA say: In 2008, 384 pilots out of a total of 6,530 applicants were selected to start training at the LFT centre. The co-pilot…was the holder a class 1 medical certificate that was first issued in April 2008 and had been revalidated or renewed every year. In August 2008, the co-pilot started to suffer from a severe depressive episode without psychotic symptoms. During this depression, he had suicidal ideation, made several ‘no suicide pacts’ with his treating psychiatrist and was hospitalized. He undertook anti-depressive medication between January and July 2009 and psychotherapeutic treatment from January 2009 until October 2009. His treating psychiatrist stated that the co-pilot had fully recovered in July 2009. Since July 2009, this medical certificate had contained a waiver…This waiver stated that it would become invalid if there was a relapse into depression. The copilot had had to pay 60,000 € to finance his part of the costs of his training at LFT [150,000€ in total]. He had taken out a loan for about 41,000 € to do so. A Loss-of-License (LOL) insurance contracted by Germanwings existed and would have provided the co-pilot with a one-time payment of 58,799 € in case he had become permanently unfit to fly in the first five years of employment. This type of insurance is contracted for all Lufthansa and Germanwings pilots until they reach 35 years of age and complete 10 years of service. The co-pilot did not have any additional insurance that would cover for potential future loss of income in case of unfitness to fly. In an e-mail he wrote in December 2014, he mentioned that having a waiver attached to his medical certificate was hindering his ability to get such an insurance policy. The BEA explain that: Pilots must declare on...

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2009 Newfoundland S-92A C-GZCH Accident: A Failure of Design and Certification

Posted by on 3:15 pm in Accidents & Incidents, Design & Certification, Helicopters, Offshore, Oil & Gas / IOGP / Energy, Regulation, Safety Culture, Safety Management

2009 Newfoundland S-92A C-GZCH Accident: A Failure of Design and Certification 12th March marks the anniversary of the 2009 loss of a Sikorsky S-92A off Newfoundland, Canada after two (of three) mounting studs, holding the Main Gear Box (MGB) oil filter failed, allowing a massive MGB oil loss. While 17 people died in that preventable accident, fortuitously one passenger, Robert Decker, survived (video of his eyewitness account). Controversially, following a failure during Sikorsky certification testing in 2002, the US Federal Aviation Administration (FAA) had allowed the certification of the type with a uniquely lax interpretation of the certification requirements for loss of lubrication testing. “Truth in politics is optional – Truth in engineering is mandatory.” Igor Sikorsky (1889-1972) Despite misleading social media statements by the then Sikorsky S-92A Project Director (albeit countered by others as mentioned by the TSB) that the MGB had been tested for 3 hours, with a genuine loss of lubricant the MGB disintegrated in just 11 minutes. A Preventable Accident The Canadian Transportation Safety Board (TSB) reported in 2011 on the accident to Cougar S-92A C-GZCH Flight 491.  The TSB said the: …mounting studs had fractured by overstress extension of fatigue cracks. Fretting and rub patterns observed on the filter housing and packing indicated that the fatigue cracking developed in the forward stud, causing it to fail, which increased the load on the aft stud leading to its failure. Such failures of MGB filter mounting studs (or bolts) is not unheard of (in these cases on Australian operated WHL Sea King Mk 50s): Source: SURVEY OF SERIOUS AIRCRAFT ACCIDENTS INVOLVING FATIGUE FRACTURE VOL. 2 ROTARY-WING AIRCRAFT by Glen S. Campbell, R.T.C. Lahey National Aeronautical Establishment (Canada, 1983). TSB state: On 06 August 2002, Sikorsky carried out its initial certification loss of lubricant test by draining the MGB and using only the remaining residual oil (approximately 1.3 gallons) then continuing operation in accordance with the requirements of AC 29-2C.  The purpose of this test, outlined in the test documentation, was to demonstrate that the S-92A transmission could provide, “continued safe operation for a minimum of 30 minutes following a complete loss of lubricating oil in accordance with the requirements of FAR 29.927(c)(1).” … Sikorsky and the FAA expected that, based on the similarities between the S-92A’s MGB and the Sikorsky S-60 [sic: H-60 / S-70] Black Hawk‘s MGB, the S-92A’s MGB would successfully operate for 30 minutes after draining the lubricating oil. The FAA indicated that the initial test was thought to be a low risk test, and Sikorsky scheduled it very late in the overall S-92A certification program. This original S-92A test matched the way other manufacturers conducted such a loss of lubrication test.  TSB explain that: EASA indicated that applicants in its jurisdiction normally complied with Part 29.927(c)(1) by draining the MGB and continuing operation with only residual oil. Prior to the S-92A certification validation it had already tested and certified at least four helicopters using this criterion. Aerossurance is aware that Canadian manufacturers also followed the same interpretation as the European manufacturers.  Unfortunately with just 1.3 gallons of oil the S-92A MGB: …suffered a catastrophic failure about 11 minutes after the test was started. TSB go on: Following the loss of lubricant test resulting in catastrophic failure, instead of taking steps to redesign the transmission to provide a 30 minute run dry capability [sic: this term is not used in regulation] for the MGB, Sikorsky re-visited the requirements...

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Step Change in Safety: Helicopter Safety Update 2016

Posted by on 7:09 pm in Accidents & Incidents, Helicopters, Human Factors / Performance, Logistics, Offshore, Oil & Gas / IOGP / Energy, Safety Management, Survivability / Ditching

Step Change in Safety: Helicopter Safety Update 2016 Step Change in Safety held a webinar on North Sea helicopter safety (covering CA-EBS, emergency egress, FCOMs and airworthiness matters) on 9 March 2016 (following on from a March 2015 event we have previously covered). Introduction Step Change is a tripartite UK offshore health and safety organisation combining companies, unions and regulators, formed in 1997.  The organisation has 5 strategic themes, each with a steering group: Asset integrity Competence & human factors Workforce engagement Simplification (and standardisation) Helicopter safety Les Linklater, Executive Director of SCinS, briefed on the activity of the Helicopter Safety Steering Group (the HSSG).  In particular he discussed the introduction of Category A Compressed Air- Emergency Breathing Systems (CA-EBS) and passenger size procedures following the UK Civil Aviation Authority (CAA) CAP1145 report published 20 February 2014. Category CA-EBS We have previously discussed at length the rapid development, certification and introduction of the Survitec Mk50 Passenger Lifejacket with a Compressed Air EBS (CA-EBS).  The earlier LAPP Jacket with a hybrid rebreather has recently been withdrawn from HUET training with the introduction of a new OPITO Basic Offshore Safety Induction and Emergency Training (BOSIET) and Further Offshore Emergency Training (FOET) standard (which we have previously discussed).  The Mk50 lifejacket is now used, however ‘wet’ CA-EBS training has not been introduced as yet. It was noted that the CA-EBS is a “fundamentally better” system than the previous hybrid rebreather and the goal is to introduce wet training. The UK regulator, the Health and Safety Executive (HSE), “perceive a risk” of barotrauma for repeated ascents from a depth of 1.5m during HUET.  This was called a “minuscule’ risk but one that that “needs to be managed”.  It was suggested during Q&A that it was originally understood that the HSE would waive certain requirements of the Diving at Work Regulations during HUET training but that a “risk averse” position is currently being taken.  Engagement on the medical requirements are still on-going. Participants made positive comments about the revised HUET training but there was support for resolving the issues to allow wet training. In the UK the Survitec Mk50 passenger lifejacket and CA-EBS in use.  Two performance reviews have been successfully held with Survitec on the Mk50 jacket. Survitec Mk51 and Viking jackets with CA-EBS are to be used for flight crew. CA-EBS implementation is estimated to have cost about £20 million across the UK workforce. Passenger Size Passenger size has also proved an implementation challenge, hence the decision to focus on bi-deltoid shoulder measurement as an appropriate single measurement which can be done by trained offshore medics.  Implementing this measurement programme was a ~£1 million investment to measure 75,000 people. Passengers classified as Extra Broad (XBR) have bi-deltoid measurement >22in. XBR passengers must seat in selected, marked seats with escape routes compatible with their size.  Over 75,000 UK offshore personnel have been measured, only 3% are XBR and none the Super XBR category.  As 30% of seats in the current fleet are XPR compatible (shaded grey in the diagram below) it is unlikely this restriction will every adversely affect any individual flight. It has been decided that only those with an initial measurement of over 20in will be re-measured every 4 years (prior to HUET training and ideally, for simplicity and efficiency, by offshore medics). There had been feedback that the XBR seating is not consistently occurring on return journeys (were Helideck Landing Officers [HLO] are...

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Shell Pernis 11.2t Ethylene Oxide Leak

Posted by on 12:01 am in Accidents & Incidents, Crises / Emergency Response / SAR, Oil & Gas / IOGP / Energy, Safety Management

Shell Pernis 11.2t Ethylene Oxide Leak The Dutch Safety Board has reported (in Dutch) on the leak of 11.2 tonnes of ethylene oxide from a overhead pipe at the 550 hectare Shell Pernis oil refinery on 30 December 2013. The leak was detected by a site worker at what is Europe’s largest refinery, surrounded by 500,000 inhabitants. Ethylene oxide is toxic, carcinogenic, ignites easily and may explode.  The DSB say their investigation shows that Shell was not prepared for such a leak of that size.  The adjacent port had to be evacuated due to the level of airborne contamination, and a water curtain used had the side effect of increasing the ground contamination. The spill occurred because the insulated pipework joints has degraded internally over 18 years.  The DSB say that Shell had assumed a 40 year design life and that the joints would be maintenance free for 20 years. Following the spill, Shell has taken a series of measures. The joints have been replaced by flanges which can be routinely inspected.  Shell now uses technical means to detect leaks in a timely manner and emergency procedures have been revised. Not The Only Leak Shell had suffered leaks of the same chemical in 2007 and 2009.  During the completion of this report, the DSB launched an investigation into the emission of another 25 tonnes of ethylene oxide at a sister plant at Shell Moerdijk.  It is alleged that this leak, following a repair in November 2015, was only discovered 2.5 months later. We have also previously reported on an earlier explosion there: Shell Moerdijk Explosion: “Failure to Learn” UPDATE 10 August 2016: It is reported that the UK Health and Safety Executive (HSE) have issued an Improvement Notice to Shell in the UK on its Clipper Southern North Sea complex of five bridge linked platforms, after one of their inspectors warned that: …“significant changes” to the Clipper installation meant there was risk of loss of containment from corrosion under insulation (CUI). In one instance, a four inch condensate line had to be shut down after it was discovered the thickness of the wall was just 2.6mm – a significant decrease on its nominal measurement of 11.1mm. A notice from the HSE also said “certain hydrocarbon containing lines” were three years behind their planned inspection date while certain lines had not been inspected for more than 12 years. But further: It was also found Shell had reduced its CUI inspection and repair programme staffing in March from 24 persons to eight people, which reduced the “ability to execute inspection and repairs in a timely manner”. In the 2008 book Resilience Engineering Perspectives, Volume 1: Remaining Sensitive to the Possibility of Failure, John Wetherall writes: …one hallmark of a resilient organisation is that it is prepared not only for its own failures those of which it can learn from others – the more resilient it is, the ‘bigger’ are the lessons it has learnt from others. Aerossurance has extensive safety and accident analysis experience.  For aviation advice you can trust, contact us at: enquiries@aerossurance.com Follow us on LinkedIn and on Twitter @Aerossurance for our latest updates. TRANSLATE with x English Arabic Hebrew Polish Bulgarian Hindi Portuguese Catalan Hmong Daw Romanian Chinese Simplified Hungarian Russian Chinese Traditional Indonesian Slovak Czech Italian Slovenian Danish Japanese Spanish Dutch Klingon Swedish English Korean Thai Estonian Latvian Turkish Finnish Lithuanian Ukrainian French Malay Urdu German Maltese Vietnamese Greek...

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Forgotten Fasteners – Serious Incidents

Posted by on 12:01 am in Accidents & Incidents, Fixed Wing, Human Factors / Performance, Maintenance / Continuing Airworthiness / CAMOs, Safety Management, Special Mission Aircraft

Forgotten Fasteners – Serious Incidents We examine three incidents where fasteners were forgotten during maintenance.  It two cases these maintenance errors resulted in parts falling from the aircraft.  In a third, a massive fuel leak occurred. Incident 1 – Twin Otter Mission Pod The Irish Air Accident Investigation Unit (AAIU) has recently reported on a serious incident that occurred on 15 August 2015 involving DHC-6-300 Twin Otter C-GSGF, used for aerial survey work by Sander Geophysics Ltd (SGL). Incident 1 – The Flight The aircraft was in Ireland for the low-level Tellus survey project of the Geological Survey of Ireland: The aircraft is equipped with three geophysical instruments which measure the magnetism, radioactivity and conductivity of the Earth below. It undertakes measurements as it flies at a speed of approximately 130 mph (approx 216km/h). The aircraft flies at 60 m (196 ft) above ground level… Survey lines are flown at a spacing of 200 m. The AAIU say: On take-off from Weston Airport, County Kildare the nose cone from the right hand mission equipment pod fell from the aircraft… The Flight Crew experienced a significant amount of yaw to the right which they felt through the flying controls. The aircraft diverted to Dublin Airport where it subsequently landed safely. There were no injuries. One of the three sensors in use was an Electro Magnetic (EM) system.  A signal is transmitted from the right hand wing tip pod and the signal is received in the left pod. Incident 1 – The Safety Investigation The AAIU say: On 14 August 2015, the day before the event, in accordance with the maintenance instructions prescribed in the [mission modification’s Supplemental Type Certificate] STC, the aircraft underwent a 125 hour Supplementary Inspection. This inspection called, inter alia, for the removal of “the EM pod nose and tail cones” and inspection of “the pod internal frames for cracks or other damage”. …the Operator’s standard practice calls for the fitting of flagging tape when parts are removed and that the flagging tape should only be removed following re-installation of the removed part(s). On this occasion the personnel involved advised the Investigation that flagging tape was not fitted. It was reported that during the EM Pod maintenance, while the nose cone was being reinstalled, a fault was detected with its sensor system. Re-installation of the nose cone was halted pending identification of the cause of the fault and consequently only the top two nose cone retaining screws were re-installed. Troubleshooting subsequently traced the origin of the sensor problem to a location inboard of the pod and the fault was rectified. The Inspection was then completed but the 14 remaining nose cone retaining screws were not re-installed. The AAIU say: All personnel who completed walkaround inspections on the morning of the event had completed a third party, computer based Aviation Maintenance Human Factors course… There is no mention of the use of more interactive or tailored training. The check was recorded in the Tech Log but it would not necessarily have been apparent that the nose cone had been removed to the crew.   The Flight Manual Supplement does have a requirement to “check that all visible attaching fasteners are installed and secure”. The Commander said that he “…there’s not any moving parts on the pods. I had a cursory look at the pods probably from about fifteen feet ahead...

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Heli-Expo 2016 Photo Report

Posted by on 12:14 pm in Accidents & Incidents, Business Aviation, Design & Certification, FDM / Data Recorders, Helicopters, Military / Defence, Mining / Resource Sector, News, Offshore, Oil & Gas / IOGP / Energy, Special Mission Aircraft, Survivability / Ditching

Heli-Expo 2016 Photo Report News from HAI Heli-Expo 2016 in Louisville, Kentucky (1-3 March 2016): Airbus Helicopters H215 Airbus Helicopters had on show the newly designated H215, formerly the AS332C1e (i.e. an enhanced, short fuselage Super Puma) and AS332L1e (the long fuselage version), to be built in Romania and aimed at aerial work, disaster relief and other missions.  The replacement of elderly SA330Js, S-61s and Mil Mi-8s being distinct targets. The Finnish Border Guard recently took delivery of its first H215, OH-HVP, with the second to follow in Apri 2016l.  It has been suggested that a major current sales target is California’s Department of Forestry and Fire Protection (CAL FIRE), which has issued a tender for 15 helicopters. Airbus Helicopters AS350 / H125 Probably one of the oddest special mission modifications on show was this AS350B3 fitted for environmental research. The so called Helicopter Observation Platform (HOP), N350UM, is owned by the University of Miami Rosenstiel School of Marine and Atmospheric Science and operated by Helicopter Express.  The aircraft was exhibited by Donaldson Aerospace & Defense as it is  equipped with a Donaldson Inlet Barrier Filtration (IBF) system. Meanwhile Vector Aerospace and Robertson Fuel Systems were exhibiting their soon to be certified (by FAA and EASA) Crash Resistant Fuel System (CRFS) for the AS350 AStar and EC130B4. This direct replacement tank features a number of safety enhancements, including the introduction of modern fuel retention technology and the relocation of certain critical components to further enhance safety and ease of maintenance. Vector worked closely with Onboard Systems to ensure that the tank remained compatible with Onboard’s cargo swing options. For more on the value of this modification see our article: Crashworthiness and a Fiery Frisco US HEMS Accident Airbus Helicopters H130 Canadian operator Phoenix Heli-Flight took delivery of a spectacularly painted H130 at the show. Airbus Helicopters H160 and H175 While Airbus did not exhibit aircraft or mock-ups of the H160 and H175 this year they did offer attendees a virtual reality experience with both. Meanwhile it has been reported that Airbus Helicopters are planning a new lean production philosophy for the H160.  ‘Major Component Assemblies’ will be produced in different locations before final assembly and flight test at Marignane in France. Production aircraft will have their tail booms produced Albacete, Spain, and main rotor blades would be produced at La Courneuve, near Paris. The central and front fuselages will be produced and pre-equipped by Airbus at its Donauworth facility in southern Germany. They will be mated together in Marignane with the main dynamic components that are also produced there. This could see the 36 week assembly process for the AS365 drop to 18 weeks for the H160, when the production line opens in 2017. UPDATE 10 October 2016: The H160 has now achieved 250 hours in flight test. Bell 505 Jet Ranger X Two Bell B505s were on display. The B505 first flew with a single, right hand side, horizontal stabiliser. The type has now a rather less elegant solution. The Bell 505 features a Garmin G1000H avionic suite. Bell 525 Relentless Bell also brought B525 Flight Test Vehicle 2 (FTV2) to the show.  The second aircraft first flew on 21 Dec 2015.  The 525 utilises fly-by-wire (FBW) controls. A third aircraft is due to join the flight test programme in the coming month, to be followed by two...

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Misrouted Engine Fuel Control Cable Hawker 800XP

Posted by on 12:01 am in Accidents & Incidents, Business Aviation, Human Factors / Performance, Maintenance / Continuing Airworthiness / CAMOs, Safety Management

Misrouted Engine Fuel Control Cable Hawker 800XP In Issue 4/2015 of TP 6980 – Canadian Aviation Service Difficulty Reports – Feedback an maintenance error involving a Hawker 800XP fuel control cable is reported: During a planned major structural inspection, the technician noticed that the no.1 engine high-pressure fuel lever cable was trapped under the cover of the electrical junction box. The box straddles the area beneath the floor. Luckily the cable was still able to move and function normally as there was only a slight cable deflection under a flexible plastic cover. The cable was inspected, found to be serviceable with no apparent damage. The cable was properly re-routed above the junction box as per the maintenance manual requirements. Transport Canada say: The mis-routing of this control cable was done at either its last replacement or re-installation from a past maintenance check or snag rectification. As it is with any primary flight or engine control, an independent inspection and dual sign-off would have been required as stated in CAR standard 571.10, maintenance release. Transport Canada Civil Aviation would like to advise all maintenance personnel that the inspection criteria includes an operational check and confirmation for correct assembly of the complete affected system. Our readers will know Aerossurance has previously discussed independent inspections several times, including: Critical Maintenance Tasks: EASA Part-M & -145 Change EC130B4 Accident: Incorrect TRDS Bearing Installation You may also find these earlier articles of interest: James Reason’s 12 Principles of Error Management Maintenance Human Factors: The Next Generation Aerossurance worked with the Flight Safety Foundation (FSF) to create a Maintenance Observation Program (MOP) requirement for their contractible BARSOHO offshore helicopter Safety Performance Requirements to help learning about routine maintenance and then to initiate safety improvements: Aerossurance can provide practice guidance and specialist support to successfully implement a MOP. Aerossurance has extensive air safety, airworthiness, human factors and safety analysis experience.  For aviation advice you can trust, contact us at: enquiries@aerossurance.com Follow us on LinkedIn and on Twitter @Aerossurance for our latest...

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Pitot Punctures Floats in Icelandic SAR Ditching

Posted by on 11:18 pm in Accidents & Incidents, Design & Certification, Helicopters, Maintenance / Continuing Airworthiness / CAMOs, Offshore, Safety Management, Special Mission Aircraft, Survivability / Ditching

Pitot Punctures Floats in Icelandic SAR Ditching The ditching of Icelandic Coast Guard Aérospatiale SA365N Dauphin TF-SIF in the Atlantic off Reykjavik on 16 July 2007 highlights the importance of avoiding protuberances that can puncture emergency flotation systems, careful configuration management and establishing emergency drills. The Icelandic Transportation Safety Board (ITSB), the RNF, issued their report in December 2010. The Accident Flight The aircraft was on a winch training mission to hoist people from the Slysavarnarfélagið Landsbjörg (ICE-SAR) 16m Arun Class lifeboat BS Einar Sigurjónsson, a life raft and from the water at a training area about 8 minutes from their base at Reykjavik’s domestic airport. The RNF say that: …arriving at the training area, the aircraft was flown in a standard pattern at 200 feet and 60 knots IAS and then descended to 100 feet and 20 knots IAS. When the training session began, the aircraft was hovered at 45-50 feet and 0-5 knots GS. At this time a power check was made and the pre-hoist checklist was completed. According to the commander’s statement, all parameters were normal and the torque was approximately 85%. The commander announced to the crew that the aircraft was in Class 3 performance and the aircraft would be ditched in case of an engine or tail rotor failure. The aircraft was operating in a light wind (10 knots) and at ISA-1 (14°C).  Being Performance Class 3 (PC3) highlights the risk of conducting live winching on an aircraft with limited One Engine Inoperative (OEI) performance. While in the hover at 45 feet, the crew commenced an operation to winch a rescue litter down to the lifeboat. About 3 seconds after the line was free from the litter the low Nr [main rotor speed] horn started to sound… [and]…the crew noticed a power loss followed by a reduction of Nr. The PF [Pilot Flying] directed the aircraft away from the ship and scanned the caution warning panel for warning lights but saw none lit. The PNF [Pilot Not Flying] looked at the Nr indicator and determined it to show Nr between 300 and 330 (Normal Nr is 355) rpm and the aircraft was losing altitude. About 10 seconds after the horn first sound, the crew deployed the floats and 7 seconds after that made a controlled ditching in water estimated to be Sea State 2-3. …the crew retarded the fuel flow control lever (FFCL) in order to shut off the engines. The pilot reported that when shutting off the right hand engine the engine seemed to be already on low rotation speed. The crew then stopped the main rotor by applying the rotor brake and then cut the hoist wire. After a short briefing the crew shut the battery off as well as the gyros.  The crew then evacuated the aircraft through the right hand sliding door and swam to a boat from BS Einar Sigurjónsson. The RNF note the evacuation was a surprisingly unhurried 4 minutes after ditching.  The floats had inflated correctly however the crew noticed when they evacuated that that the front floats were rubbing against the pitot tubes and shortly after the forward chamber of the right hand front float deflated. The aircraft capsized approximately 18 minutes after ditching. The Safety Investigation The helicopter was fitted with a Cockpit Voice Recorder (CVR), though not a Flight Data Recorder (FDR).  Acoustic analysis of he CVR showed that one...

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Falcon 7X LOC-I Due To Solder Defect

Posted by on 1:49 pm in Accidents & Incidents, Business Aviation, Design & Certification, Safety Management

Falcon 7X LOC-I Due To Solder Defect On 25 May 2011, Dassault Falcon 7X business jet, HB-JFN, operated by Jet-Link, suffered a pitch trim runaway that caused a 40° pitch up, rapid climb and temporary Loss of Control Inflight (LOC-I) over Malaysia. First flown in 2005 and certified in April 2007, after a 590 flight, 1600 flying hour test programme, the 7X features a fly-by-wire (FBW) control system.  This Digital Flight Control System (DFCS) and the Falcon family’s EASY (Enhanced Avionics SYstem) flight deck design draw on Dassault’s 30 years of military fighter experience, especially its Rafale and Mirage 2000. The type had accumulated 75000 flying hours at the time of the incident. The French Bureau d’Enquêtes et d’Analyses (BEA), to whom the investigation was delegated, has now reported (in French) on this serious incident (commenting that the long duration was necessary to examine the organisational factors). The Incident Flight While descending through 13000 feet at the end of a positioning flight to Kuala Lumpur, over 15 seconds the elevator pitch trim began to move from neutral to the full nose-up position. The First Officer (Pilot Flying), a former military pilot with experience on Mirage IV and Mirage 2000, put the aircraft into a steep right-hand bank to aid recovery partially replicating the ‘palier-ressource’ military manoeuvre (which involves approaching a target in level flight before pulling up at 30° pitch to release the weapon, and then banking to 90° to reduce pitch and escape). At two points (for 9 and 12 seconds) both the Commander (Pilot Non-Flying) and the First Officer were simultaneously using their side stick.  The First Officer used the priority button to override the Commander’s inputs and asked him to stop.  The pitch subsequently decreased, as did the load factor (from a maximum of 4.6 g to less than 1.5 g). After about 2.5 minutes the crew regained control and landed safely. The aircraft had however climbed to 22500 feet. Immediate Response The incident prompted such concern that the next day that the European Aviation Safety Agency (EASA) published an Emergency Airworthiness Directive (EAD), prohibiting further flights by the Falcon 7X fleet until further notice.  A further Airworthiness Directive (AD), in two stages, permitted operations to resume with modifications and operational limitations.  A third AD with modifications and operational tests followed. The Safety Investigation The BEA found that a defective ‘cold’ solder joint at a pin of a component of the Horizontal Stabilizer Electronic Control Unit (HSECU) led this computer to sending erroneous signal to the actuator driving the horizontal stabiliser trim (HRT) and a simultaneous failures of monitoring channel which were not detected. The solder had not reached an adequate temperature because the board had acted as a heat sink, resulting in micro-cracking.  They highlight a similar, but unconnected case in 2007 (Airbus A321 I-BIXK that suffered a braking failure after similar solder defects in its Brakes and Steering Control Unit). A number of contributory factors are identified by the BEA.  One is the non-detection of the production fault.  They also comment on the HSECU supplier’s Failure Modes and Effects Analysis (FMEA) which was not suitably comprehensive.  They note that this FMEA was not subject to detailed review by the aircraft Type Certificate (TC) Holder.  The TC Holder’s System Safety Assessment (SSA) in accordance with 25.1309, being partly based on that FMEA, was therefore incomplete. The BEA also reference safety assessment lessons from an Australian Transport Safety Bureau (ATSB) report into an upset involving a A330 VH-QPA in 2008 (in that case not...

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